Table 3 Use of new method to improve the process.

From: Enhancement in production efficiency using DMAIC methodology of six sigma

Defect

Identified the root cause problem

Method

Pitting

The top and bottom die is not properly lubricated during working time

By training the oilman to lubricate the die after 3–4 pieces of manufacturing

Die and billet are overheated during working time.

By maintaining a proper temperature range, depending on the product size

Reusing of used billet

Do not use more than two times a billet

Total length undersize

Use of more packing plate

Do not reuse more than three packing plates

Less billet weight

Proper billet cutting by the cutting machine and weighing machines provided for efficient control

Not the proper function of the ejector system

By proper lubrication in the ejector system and by using a new ejector pin in the ejector system. Ejector pin is standardised depending upon the length of the product or by changing the ejector pin as per the preventive schedule

Un-filling defect

Die setting not proper

Use of a bolt and a clamp

Low air pressure

By providing a pressure gauge in the machine

Undersize billet

Proper billet cutting by band saw machine and weighing machines to be provide better control.

Flash defect

Untimely change of die blocker

By changing the top blocker and bottom blocker after 6500–8500 pieces of manufacturing

Material overlaps

By maintaining proper clearance between the top and bottom blocker dies and maintaining proper temperature

Die shortage

Maintain the single minute exchange die properly.

Bend defect

Unstandardised die punch

By using a new die or fewer than three packing plates

Die loss during production

Die change by a preventive schedule. Top and bottom die change in 6500–8500 pieces of manufacturing